Saturday 21 March 2020

16. Karmann Ghia Restoration - Big Trouble with the front Axle







Time to look at the front axle and like most projects I started with great enthusiasm. So I stripped the front axle of all the brakes and suspension parts and removed the axle beam from the chassis. 





My next job was to remove 50 years of road dirt from the axle beam which took a very long time and then finally give the beam a coat of rust converter and then chassis black.






It was not until I had done all of this work, and laid the axle down on the bench that I noticed that the axle appeared to be BENT!
Careful measurement confirmed that  the ends were indeed bent back from the centre by about 5mm. Disaster! I immediately went on the internet to see if it was a big problem. The answer was that the axle must be straight. The good news was that the internet said that, with a good press, it was possible to straighten it.

So I took the axle to my friends workshop and we carefully supported the ends  of the axle on wood and then applied pressure to the centre struts of the axle, via another piece of wood in his press.

After a fair bit of pressure, the axle tubes straightened and we checked the tubes with a straight edge to ensure they were now level.


We were feeling pretty pleased with ourselves that we had achieved until I got the axle back to my workshop and I happened to turn the axle over and spotted what had happened to the axle end caps.

They had both crushed, under the weight of the press and were now beyond use. All of that work was now wasted and I had to find a replacement front axle.

That was not as easy as I thought, as no standard replacement axles were available, even in the USA.

So, in the end, I had to settle for an adjustable front axle. It's basically the same but the centre clamp points for the torsion bars are adjustable, allowing you to lower the suspension, if desired. Now as I don't want to lower my suspension these adjusters will just have to be set at the top (standard position). But there it is, fitted to the chassis and now I've got to rebuild it.





Stripping the old axle revealed another problem. Two of the leafs in the torsion bars were broken in the top tube. I doubt if I would have ever found that had the axle not been replaced. So now I had to order new torsion bars.


Along with the new the new torsion bars, I ordered all new ball joints and track rod ends. Now here comes the next mistake. The trailing arms cleaned up beautifully and I took them, along with the new ball joints back to my friend's workshop to have the old ball joint pressed out and the new ones pressed in. It took 8 tons of pressure to do this.







I took them back to my workshop and fitted them  onto the new axle along with the renovated stub axles and new shock absorbers.

I wasn't over concerned, as everything was new, but the ball joints did seem very tight and so, just to be sure, I went back on the internet only to discover another problem.

The ball joints have notches in their caps and, according to the web, these notches have to be orientated front to back on the car. I had noticed the notches but had not checked what they were for. Now I had to go back to the car and check where the notches had finish up after we had pressed them in.

As luck would have it, three of the four ball joints were in the right orientation (Pure luck) but the upper right was 90 degrees out. So I had to order another ball joint and strip that side again, take it back to my friend, and replace the ball joint again.  I didn't want to chance refitting the first one again in case two lots of pressing had damaged it.

It was about time I had a bit of luck and that came with the steering box. I fully expected to have to overhaul it. However  inspection revealed absolutely no wear and no play. So it was just a case of cleaning it up and fitting it to the axle. The new axle has no mounting lugs, so I've had to estimate it's position and I'll have to adjust that once the body and steering column are back in place.


Time to clean up and refit the anti-roll bar with all new rubbers and clamps. No great problems there in fact I think it fits better that it did originally.

What was difficult was refitting the grease nipples, which would not cut into the holes in the new axle and in the end, I finished up fitting new ones. I also treated myself to a new , air powered, grease gun and I've been pumping grease into this new axle for some time now and still haven't managed to fill the new empty tubes yet. I now need to buy more grease.


It's now time to renovate the track rods and replace the track rod ends. No great problems here.


And complete with a new steering damper they were soon fitted.






Now, at last I could fit the brake back plates and the new discs, complete with all new wheel bearings and oil seals.

One problem, after fitting the discs was that the grease caps, that came with the discs didn't fit over the bearing clamp nut and the old caps are not fit to use. So I've had to put a new pair on back order.





Now it had been my intention to paint the new brake caliper "Red". However, when I opened the boxes, I found, to my surprise, that the new calipers were chrome plated. Now I don't know how good the chrome is but I felt it was worth leaving them as they are and see how they weather. I have already bought the red caliper paint, so if they do begin to rust I can always paint them later.









My next job is to replace the rear suspension, torsion bar and cap rubbers, that I have ruined, and then I'm going to reinstall the gearbox, that has already been overhauled.


You can contact me on hopcroftscoot@gmail.com

Copyright 21.03.20 all rights reserved.

My Other Blogs:
1961 BSA A10 Super Rocket Motorcycle:
http://60sclassicmotorbikes.blogspot.co.uk/2012/07/before.html

1961 Ariel Arrow Super Sport Motorcycle :
http://60sclassicmotorbikes.blogspot.co.uk/2014/01/1961-aerial-golden-arrow-restoration.html

Miniature Land Rover Defender:
http://miniaturelandrover.blogspot.co.uk/2016/02/1-miniature-land-rover-defender-idea.html?view=timeslide

Motorcycle Trailers / Caravans:
http://motorcycletrailersandcaravans.blogspot.co.uk/2018/01/1-motorcycle-trailers-problem.html


Sunday 8 March 2020

15. Karmann Ghia Restoration - Chassis Rebuild


At last, the chassis is back in my own workshop. Now I can start the mechanical restoration, to make the chassis ready for when the body arrives.







So the first thing to do is clean up all the areas that are still original and that means hours of wire brushing, cleaning and painting.









After removing 50 years of road dirt, the next job was to apply a coat of rust converter and then once dry a coat of "chassis black" paint. I'm a particular fan of Chassis Black as it provides excellent thick metal coverage combined with good road dirt protection and a good gloss finish






My next job is to raise the rear suspension. 
If you look at this original picture, you can see that the front of the car is high and the back is low. Now it is my intention to fit a tow bar to this car when it is done and tow my motorcycle trailer with it. This will enable me to show both the car and two of my motorcycles at vintage rallies. I had lifted the back of the car on it's suspension to see how much higher it needed to be for it to sit level before I started to strip the car and it appeared to need about 63mm (2.5").

After reading about the rear torsion arm information on the internet, I found that one notch on the inner splines actually changes the height of the car by exactly 63mm. This can be reduced by moving the outer splines one notch should I find that it's too much when I finally put the car back on the chassis.

So, after removing the rear brakes, Unbolting the trailing arms and swinging them downwards, I removed the torsion bar end caps. My next problem was how to release the tension on the spring plate and after turning the torsion bar one click, how to pull the spring plate back up again onto its rest.

Now normally, with the weight of the car on the chassis, it is just a case of using a jack to push the spring plate back up again. But with no weight on the chassis, all a jack does is lift the whole chassis. So I had to devise a simple spring compressor as shown on this picture.

This worked great, but I should have investigated the reassembly instructions further, because I should have refitted the end caps before retensioning to torsion bar.

The result was that, with the spring plate under tension and back on its rest, the end cap would not line up with its fixing holes. I then made another bad decision. I decided to make another tool to force the end caps back on.

This turned out to be a very bad decision, because inside the end cap is a large rubber mounting doughnut. The four threaded rods forced the cap on OK but crushed the rubber doughnut and damaged it beyond use. So I have had to strip it again and I am now awaiting the arrival of two new doughnuts. After reading further I discovered that what I should have done is refit the end cap before retensioning the torsion bar. But you live and learn.





Anyway I left the end caps where they were for the time being and proceeded with the reassembly of the rear brakes. 

The first job was to clean up the back plates and rustproof and paint them. Next the shoes and springs were cleaned along with the brake adjusters. The back plate was then clamped into place with the axle end caps fitted with new oil seals and then the new wheel cylinders and cleaned brake shoes could all be fitted. 













The good news was that the brake linings were in excellent condition and the drums only needed cleaning and painting.













It's now time to look at the pedal cluster and like everything on the car, it's showing it's age. So a complete strip was necessary. Some parts needed straightening and then they all needed painting and lubricating with copper slip grease.





Now with all new rubbers fitted it could be fitted back onto the chassis. Before doing that I remembered an old modification that we used to do back in the 1960's and that was to drill a small hole in the end of the hook where the clutch cable hooks on. The idea of this is that, when fitting, you hook the clutch cable over the hook and then fit a small split pin through the drilled hole. This stops the clutch cable slipping off the hook whilst fitting.


 
 Now I could fit the new dual circuit master cylinder and all of the new brake pipes. 















I decided that, with a car of this age, it was a good idea to replace all brake components and so all flexible pipes were also replaced just to be on the safe side.







Well that's it for this episode but on the next one there is big trouble with the front axle.

You can contact me on hopcroftscoot@gmail.com

Copyright 08.03.20 all rights reserved.

My Other Blogs:
1961 BSA A10 Super Rocket Motorcycle:
http://60sclassicmotorbikes.blogspot.co.uk/2012/07/before.html

1961 Ariel Arrow Super Sport Motorcycle :
http://60sclassicmotorbikes.blogspot.co.uk/2014/01/1961-aerial-golden-arrow-restoration.html

Miniature Land Rover Defender:
http://miniaturelandrover.blogspot.co.uk/2016/02/1-miniature-land-rover-defender-idea.html?view=timeslide

Motorcycle Trailers / Caravans:
http://motorcycletrailersandcaravans.blogspot.co.uk/2018/01/1-motorcycle-trailers-problem.html